114) In this case I started by repairing the rocker endcap first. Notice that the patch is larger than what is required? That is
because it is easier to weld up beyond the end of the original metal and grind the patch back to the correct
dimension, than it is to stop a weld at the exact edge you need.
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115) Here it is after the butt-welding process and a little bit of grinding. I use 36 grit disks on my air grinder to get
the welds flat as possible. If you do it right, you will not need to use any filler.
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116) Next came the side panel bottom. The patch needed to have a couple bends in it to match the original contour lines, which
you can see marked on the patch (but not bent yet).
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117) The bends I made in a bench vise. Here it is welded in.
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118) Here is the last patch. Again the patch needed to have a bend in it to match an original contour line.
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119) Here it is all welded up. You may notice the front part of the A-pillar where it meets the rocker. There was a small rust hole that
opened up to a larger one after sandblasting. I was able to just plug weld the hole instead of having to patch it.
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120) In this last picture I hit everything with some weld-though primer to temporarily protect my work from rusting and to get a
good visual of my work. The lines in the patches came out pretty good, don't you think?
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